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author | Stefan Richter <stefanr@s5r6.in-berlin.de> | 2010-08-16 22:13:34 +0200 |
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committer | Stefan Richter <stefanr@s5r6.in-berlin.de> | 2010-08-19 20:28:25 +0200 |
commit | a481e97d3cdc40b9d58271675bd4f0abb79d4872 (patch) | |
tree | c860d626fbee5f1fb2bc9511fa7fb3c586801c56 /drivers/serial/atmel_serial.c | |
parent | 6c74340bce253ea95c9ee801b3c411a333937edf (diff) |
firewire: sbp2: fix stall with "Unsolicited response"
Fix I/O stalls with some 4-bay RAID enclosures which are based on
OXUF936QSE:
- Onnto dataTale RSM4QO, old firmware (not anymore with current
firmware),
- inXtron Hydra Super-S LCM, old as well as current firmware
when used in RAID-5 mode, perhaps also in other RAID modes.
The stalls happen during heavy or moderate disk traffic in periods that
are a multiple of 5 minutes, roughly twice per hour. They are caused
by the target responding too late to an ORB_Pointer register write:
The target responds after Split_Timeout, hence firewire-core cancels
the transaction, and firewire-sbp2 fails the SCSI request. The SCSI
core retries the request, that fails again (and again), hence SCSI core
calls firewire-sbp2's abort handler (and even the Management_Agent
register write in the abort handler has the transaction timeout
problem).
During all that, the process which issued the I/O is stalled in I/O
wait state.
Meanwhile, the target actually acts on the first failed SCSI request:
It responds to the ORB_Pointer write later (seen in the kernel log as
"firewire_core: Unsolicited response") and also finishes the SCSI
request with proper status (seen in the kernel log as "firewire_sbp2:
status write for unknown orb").
So let's just ignore RCODE_CANCELLED in the transaction callback and
wait for the target to complete the ORB nevertheless. This requires
a small modification is sbp2_cancel_orbs(); it now needs to call
orb->callback() regardless whether fw_cancel_transaction() found the
transaction unfinished or finished.
A different solution is to increase Split_Timeout on the local node.
(Tested: 2000ms timeout; maybe 1000ms or something like that works too.
200ms is insufficient. Standard is 100ms.) However, I rather not do
this because any software on any node could change the Split_Timeout to
something unsuitable. Or such a large Split_Timeout may be undesirable
for other purposes.
Signed-off-by: Stefan Richter <stefanr@s5r6.in-berlin.de>
Diffstat (limited to 'drivers/serial/atmel_serial.c')
0 files changed, 0 insertions, 0 deletions